Global Weather Phenomenon-Natural/Technological Disasters-Space Events-Epidemic/Biological Hazards-
Nuclear Events :
News Affiliate of Family Survival Protocol.com
Damage
to an electrical transformer caused one reactor to shut down
automatically at a northern Illinois nuclear power plant over the
weekend. Unit 2 at the Dresden Nuclear Station shut down Saturday
morning, and it remained offline on Sunday as crews worked to fix the
damage. Dresden spokesman Robert Osgood says the problem is on the
non-nuclear side of the plant. He says the plant responded as expected,
and there was no safety threat. He says a second reactor is operating
normally, and electrical customers will not be affected. The plant is in
Morris, about 60 miles southwest of Chicago,
The
plant shut down in October 1978 and is currently in SAFSTOR. The
Decommissioning Plan was approved in September 1993. No significant
dismantlement activities are underway. Isolation of Unit 1 and Units 2
and 3, is complete. All spent fuel from DNPS Unit 1 that was previously
stored in the Unit 1 SFP, the Unit 1 fuel transfer pool, and the Unit 2
SFP has now been transferred to the on-site Independent Spent Fuel
Storage Installation (ISFSI). Currently, 108 spent fuel assemblies and
one fuel rod basket from Unit 1 are stored in the DNPS Unit 3 SFP.
During the SAFSTOR period (through 2027), the Unit 1 facility will be
subjected to periodic inspection and monitoring. These activities will
include condition monitoring of the ISFSI, ongoing environmental
surveys, and maintenance of equipment required to support the SAFSTOR
condition of the facility. Security will be maintained as part of the
site protected area boundary for DNPS Units 1, 2, and 3 during this
period. The licensee plans that decontamination and dismantlement of
DNPS Unit 1, including removal of any remaining Unit 1 spent fuel that
is stored in the Unit 3 SFP, will take place from 2029 through 2031.
Major components, including the nuclear steam supply system and the
turbine-generator machinery, will be decontaminated as needed, and
removed at this time. Other systems and components will also be removed,
packaged and disposed of; the associated buildings will be prepared for
demolition. A four-year site restoration delay will follow the major
decontamination and dismantlement of DNPS Unit 1 to allow for the
decontamination and dismantlement of Units 2 and 3, with completion of
these activities tentatively planned for 2035. Site restoration is
planned for in 2035 and 2036, with the demolition of the remaining
structures and removal of contaminated soil. The licensee plans to
conduct a final site survey in late 2036. The licensee will monitor the
DNPS ISFSI complex with site security and periodic inspections until
final transfer of the spent fuel to the Department of Energy for
disposal.
Dresden Unit 1 produced power commercially from 1960 to
October 31,1978. The unit had a history of minor steam leaks and erosion
in steam piping in the early and mid-1960s. There were also fuel
failures during the period of September through December of 1964 and
other times which, although not leading to off-gas releases above
limits, did cause redistribution of radionuclides from the fuel to other
parts of the primary system. Several systems in the plant used
admiralty brass (Cu-Ni) heat exchange surfaces, including the Main
Condenser. Most of these were taken out of service and replaced with
stainless steel tubing. In the sixth partial refueling, the condenser
was re-tubed from admiralty brass to 304L stainless steel. The use of
Cu-Ni surfaces did lead to translocation and deposition of corrosion
products throughout the operating systems. The use of carbon steel in
the Secondary Feedwater System may have also contributed to the elevated
corrosion radionuclide levels. These foregoing events led to the need
to perform a chemical decontamination of the Primary System. The Unit
was taken off-line on October 31, 1978, to backfit it with equipment to
meet new federal regulations and to perform a chemical decontamination
of major piping systems. While it was out of service for retrofitting,
additional regulations were issued as a result of the March 1979
incident at Three Mile Island. The estimated cost to bring Dresden Unit 1
into compliance with these regulations was more than $300 million.
Commonwealth Edison concluded that the age of the unit and its
relatively small size did not warrant the added investment. In 1984,
chemical decontamination of the primary system was performed and 753
curies of Cobalt-60 and 12.4 curies of Cesium- 137 were removed. This
decontamination was completed and activities began shortly thereafter to
prepare the facility for decommissioning. In July of 1986, the NRC
revised the Dresden Unit 1 license to possess-but-not-operate status.
The United States Nuclear Regulatory Commission (NRC) approved Revision 3
to the Dresden Unit 1 Decommissioning Program Plan on September 3,
1993. In 1998, the Decommissioning Program Plan was revised to the
current Defueled Safety Analysis Report (DSAR) format.
3.0 Major Technical or Regulatory Issues
None.
4.0 Estimated Date For Closure
12/31/2036
Page Last Reviewed/Updated Thursday, February 20, 2014
The
center of this Toxic Plume is located approximately 60 miles southwest
of Chicago, Illinois. This plume is produced by 2 reactors located at
the Dresden Nuclear Power Plant site. The reactors that produce this
plume have 1,734 Mega Watts of radiation generating power. There is a
total of 1,050 tons of Highly Toxic Radioactive spent fuel stored at
this Nuclear Power Plant. The Dresden Nuclear 1 reactor has been forced
into permanent shut down, leaving the plant in a virtually unattended
state. During one winter, this unit experienced containment flooding to
the service water system, due to freeze damage. It was determined that a
similar threat to Spent Fuel Pool integrity. Tritium leaks at the other
units in this plant are treated with the same lack of concern that
Nuclear Power corporations give all leaking radiation.
No comments:
Post a Comment
Hello and thank you for visiting my blog. Please share your thoughts and leave a comment :)